Overall, we were not entirely satisfied in our result. It would've been nice if the mechanism worked and the avocado pit had The goal was for the avocado pit to be effectively been removed and this did not happen. The linkage connecting from the the end of the knife handle to the actuator was unstable and the servo that powered the linear motion was not powerful enough. Lastly, the avocado grip and holder was too small and unfortunately squished the avocado.
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